Hi all, finally get to start this thread - I purchased JSK's Dark Grey SX/4 Sport about 2 months ago. Ended up having transport issues and delay after delay. However, last weekend it finally made it to me! I have never before owned an Eagle, but in person it's an amazing machine.
I will begin posting updates and progress pictures as I get her back to life. I'll start the log now, beginning with an email I sent to Jerry.
- December Saturday 8th / Sunday 9th -
Drained the old gas out, it looked like black coffee and didn't even smell like gas anymore! Probably the nastiest stuff I've dealt with in a while. After getting that done, put some fresh gas in, popped off the fuel filter and turned her over, in turn that pushed all the old nasty fuel from the lines until nice clean fuel was spewing out.
From there I could get her to start with fuel into the carb, would idle but die quickly. Took apart the little valve with the needle, found it clogged with that green slime you mentioned. Cleaned that up and it still wouldn't idle. Ended up checking the fuel filter, fuel was feeding to it fine, but the end into the carb was barely flowing. Bought a new fuel filter, started her, idled perfect. Made sure I filled the coolant up, it was empty. Let her run for a good 20-30 minutes.
Turned it off and took a break. Came back out for a test drive. Started up perfectly, hopped in and went to the sandwich shop. Very responsive, no lag, shifts great - However I was getting a strange vibration which at first I thought was a sticking brake, but wasn't positive. Made it home and called it a night. I couldn't believe the attention I was getting at stop lights, people were giving me the "What is that" look.
Woke up on Sunday, decided to go on a little run to diagnose the issue. Made it about 2 miles with the shake when I heard a clank and the vibration went away...not good. I got out to take a look and found the rear drive shaft had disconnected and it was flopping around on the exhaust. Ended up slugging it back to a Napa parking lot, heated it up a bit only pulling with the 2 front wheels and it vomited some coolant out. I called a tow and had her dropped at my mechanic and she is still at the shop being inspected. Fixing the driveshaft for sure, getting a new radiator and any other needed fixes.