Tonight didn't go as planned but at least....... she is running again!
On the first start, the hose for the intake manifold was not seating properly and peed coolant all over the place. I fixed that and tried again. Once up to temp, the lower radiator hose let loose and coolant all over again. So I pulled the power steering resivoir and found the lower rad hose fitting was rusted up. I cleaned it off really good, installed the hose, refilled the radiator and tried again. This time success! No leaks.
I also adjusted the fuel mixture by turning both screws all the way in. Then I backed them out two full turns of the screwdriver. I also lowered the curb idle until the dizzy advance stopped pulling vac and adjusted the timing to 8 degrees. Now when I plug the vac line into the dizzy, the engine speed does not change at idle which is exactly what should happen.
It will be another week before I can drive it, but all should be well now.